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Case Study : Loose Parts

During January / February 1999, various diagnostic technology and techniques developed at the EPRI M&D Center for Generator Transformers were demonstrated jointly by EPRI M&D, CENPEEP and Plant teams. A PDM survey was performed on the Generator Transformers at one of the plants. These transformers were 270 MVA three phase step-up transformers, oil cooled, and OFAF type.

The survey in Feb 99 indicated the presence of loose parts which were externally source located, at load, indicating an internal anomaly near the bottom on the W-phase low voltage side. (LV side, bottom location 3 & 4). This location of maximum RMS levels of ultrasonic activity was identified with the help of Ultrasonic contact test equipmebnt (5550 Fault Detector) by monitoring ultrasonic RMS levels displayed on the equipment and listening to the ultrasonic signal, converted to an audible signal, by laying out a grid. The continuous and cyclic nature of ultrasonic activity, and the normal dissolved gas in oil levels indicated an absence of detectable partial discharge. Vibration spectra (peaks at multiples of odd frequencies: 3X, 5X etc.) taken at the location indicated the fault to be a possible loose part. At the bottom most portions, high ultrasonic activity was also present, and suspected due to flow induced vibrations.

In order to know the condition of the transformer and calibrate the data an opportunity was availed in April 99, during the overhaul of the unit. The manufacturer opened the transformer and found a broken fiberglass mounting nut & bolt used for mounting the Weidmann Board lying at the bottom of the transformer tank. The Weidmann board was thus found dismounted from the mounting bolt at the bottom side on the LV side below W-phase, the same location where loose part was suspected during the PDM survey earlier. The board was also loose from the top and was vibrating. If this condition continued the board would have sheared off from its mountings over a period of time. After the inspection, the board and nut / bolt were repaired and restored to original condition. The details are shown in figure below.

image1.gif

The follow-up survey in May 99, indicated reduced levels of ultrasonic activity on all sides; reduced levels of vibration; a major reduction of ultrasonic activity at the defect location, and the absence of loose part characteristics in the vibration spectra. At the bottom most part, expected flow induced ultrasonic activity was observed where the oil flow pipe is located.

The loose board itself was not expected to lead to any damage or loss of performance of transformer. The shearing off of the board would have caused secondary damages to the coil, the extent of which would depend on the location of shear, sharpness of shear edges, and angle at which the coil is hit. The probability of damage to coil is difficult to estimate but can not be ruled out. Assuming minimum secondary damages, and further damage to the board, (its shearing off) could have caused minimum loss of generation of five days (about 20 million units at about 85% PLF costing about Rs 40 million, $910K US Dollars) apart from cost of labor and material.

In this context, the survey in February 99 could correctly predict loose parts and follow up survey confirmed the restoration. This experience has given confidence to both the station and manufacturer in the benefits achievable using the techniques, and has proven to be a good confidence builder.

This case study illustrates the benefits of using multiple technologies for arriving at equipment condition making decisions based on periodic surveys, which include the use of vibration analysis in identifying the nature of fault.

 
 
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